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HomeMy WebLinkAboutWater Designs & Fire Flow AnalysisWater Design Fire Flow Analysis Report for Wellborn Business Park Phase 1 & 2 College Station, Texas February, 2012 Schultz Engineering, LLC TBPE Firm Registration No. 12327 2730 Longmire, Suite A College Station, Texas 77845 979.764.3900 F-12327 SCHULTZ ENGINEERING, LLC. /7 Water Design Fire Flow Analysis Report for Wellborn Business Park Phase 1 & 2 College Station, Texas February, 2012 Rev. May, 2013 Prepared Bv.' Schultz Engineering, LLC TBPE Firm Registration No.12327 2730 Longmire, Suite A College Station, Texas 77845 979.764.3900 F-12327 SCHULTZ ENGINEERING, LLC. General Information Location: Wellborn Business Park is located on McCullough Road, east of Wellborn Road. General Note: An 8" water line will connect to the existing 10" water line along McCullough Road. A 6" waterline will connect to the 8" line and extend into the property. Land Use: Commercial/Office Design Criteria/Analysis Primary Water Supply: Existing 10" water line along the McCullough Road, Domestic Demand: Max. Demand Flow: 58.4 gpm See Exhibit D - Fixture Unit Count Fire Flow: 1,500 gpm — Maximum building size for a hydrant flow of 1500 gpm is 5900 sf for type II-B Construction. All buildings proposed for this project are less than 5900 St. A flow test from an existing hydrant was used to compute the residual pressure to use in the WaterCad computer model. Flow Hydrant: Proposed FHl & Future FH2 Flowrate: Scenario 1: 1500 gpm —FHl —Phases 1&2. Scenario 2: 750 gpm each for FHl and Future FH2 for future development of the site after Phase 2. Exhibits: Exhibit A — Water System Layout — Scenario 1 Exhibit B — Water System Layout — Scenario 2 Exhibit C — Water System Fire Hydrant Flow Test Report Exhibit D — Fixture Count Determination Exhibit E — Pipe and Junction Analysis — Domestic Demand Exhibit F — Pipe and Junction Analysis — Fire Flow Demand Conclusion The proposed 8" & 6" water lines are in accordance with the BCS Water Design Guidelines. This report provides the results of the water system analysis under the fire flow & domestic conditions for the proposed commercial buildings. The pressure and velocity values are computed by the WaterCad software. The lowest residual pressure in the system with the fire flow and domestic demands scenario 1(1,558 gpm) is 38.5 psi and scenario 2 (808 FH 2 & 750 FH 1) is 33.7. The lowest residual pressure in the system with only the domestic demand (58 gpm) is 54 psi. Each of these pressures exceeds the 20 psi and 35 psi minimum pressure requirements. The maximum velocity in all pipes is less than 12 fps. The maximum velocity in the system will be 9.94 fps in 8" pipe P-4 with a fire flow of 1,500 gpm. R_2 0 THE GARDENS SUBDIVISION J-2 EXISTING 10' N WATERLINE ROPOSED FH 1 1500 GPM C J-3 Q' B' PROPOSED 0, WATERLINE _ — — — v P R�2 WELLBORN LANDING SUBDIVISION �oW z G`2` EXISTING 10' FUTURE FH 2 WATERLINE �J Gyl � 3 E%ISTING FH 2 WELLBORN BUSINESS PARK i a A EXISTING FH 1 _1 SahUltzEn ineering,LLC WELLBORN WATERLINE SCA" EXHIBIT "` BUSINESS PARR ` — v^b �n �+ . u.r u +• COLMOX STATION, TXXAS LAYOUT ,unn aYn_ ma a nw +n q Jlt 1i-ia mas ,u."o,,.,a R 2 q THE GARDENS SUBDIVISION J-2 EXISTING N WATERLINE PROPOSED FH I PROPOSED FH 1750 GPM y 750 GPM J-3 8' PROPOSED 6, WATERLINE — — — — v P Q,2 WELLBORN LANDING SUBDIVISIONEXISTING POP° , FUTURE FH 2 750 GPM JO`�GP WATERLINE �J J 3 EXISTING FH 2 WELLBORN BUSINESS PARK i a EXISTING FH 1 -I SCALE EXHIBIT Schultz En ineering,LLC WATERLINE .. WELLBORN + — Mm" W ,.,b,ll, BUSINESS PARK '""'^ •� 011 � COUJON STATION, TNXAS LAYOUT �+ +n �rcr +n n-in m. uu ru xuo „-n EXHIBIT C SCHULTZ ENGINEERING, LLC FIRM #12327 WATER SYSTEM FIRE HYDRANT FLOW TEST REPORT Date: June 30, 2009 Water System Owner: Wellborn SUD Development Project: Wellborn Landing Subdivision — Wellborn. Texas Flow Test Location: Fire Hydrant on McCullough Road Nozzle size (in.): 2.5 Pitot Reading (psi): 55 Flowrate (gpm): 1,245 Discharge Coeff: (c) = 0.90 Flowrate Formula: Q=29.84cd2p1/2 c = discharge coeff. d = orifice size (in) P = pitot pressure (psi) Pressure Gauge Location: Fire Hydrant at the Intersection of Live Oak and Church Static Pressure (psi): 60 Residual Pressure (psi): 56 Computed Discharge at 20 psi Residual Pressure: OR = 4,330 gpm Discharge Formula: QR = QF X (hr0.54/hf .54) Note: The flow test and report were prepared in accordance with NFPA 291. Report Prepared by: Joseph P. Schultz Others Present: Stephen Cast — Wellborn SLID Exhibit D Fixture Count Determination (Plumbing Code) Fixture Unit Value Fixture Type # of Fixtures I and M-6.- I1..:. Water Closet 1 wa vnna 5 5 Lavatory 2 2 Service Sink 1 3 3 Total = 10 'Demand = 14.6 GPM `The demand is calculated per building. There will be 4 buildings for a total domestic demand of 58.4 Exhibit E WaterCAD Analysis Summary Junction Analysis - Domestic Flow for Commercial Building Junction Elevation (ft) Total Demand (gpm) Pressure (psi) EXISTING FH 1 332 0 58.8 EXISTING FH 2 329 0 60.1 J-1 337 0 56.7 J-2 338 0 56.2 1-3 338.7 0 55.9 PROPOSED FH 1 338.7 0 55.9 PROPOSED FH 2 343.1 58 54 Exhibit E WaterCAD Analysis Summary Pipe Analysis - Domestic Flow for Commercial Building Pipe Number Length (ft) Size (in) Material Hazen- Williams C Flow (gpm) Velocity NO P-1 651 8 PVC 150 11 0.07 P-2 496 10 PVC 150 11 0.04 P-3 144 10 PVC 150 -47 0.19 P-4 82 8 PVC 150 58 0.37 P-5 5 8 PVC 150 0 0 P-6 292 6 PVC 150 58 0.66 P-RES1 11 10 PVC 150 Al 0.04 P-RE52 11 10 PVC 150 47 0.19 Exhibit F WaterCAD Analysis Summary Junction Analysis - Fire Flow for Commercial Building - 500 gpm - FH 1 & FH Junction Elevation (ft) Total y Demand (gpm) Pressure (psi) EXISTING FH 1 332 0 45 EXISTING FH 2 329 0 45.9 1-1 337 0 42.3 J-2 338 0 42.4 J-3 338.7 0 40.5 PROPOSED FH 1 338.7 750 40.4 PROPOSED FH 2 343.1 808 33.7 Exhibit F WaterCAD Analysis Summary Pipe Analysis - Fire Flow for Commercial Building - 1 500 FH 1 & F Pipe Number Length (ft) Size (in) Material Hazen- Williams C gpm Flow (gpm) H 2 Velocity (ft/s) P-1 651 8 PVC 150 287 1.83 P-2 496 10 PVC 150 287 1.17 P-3 144 10 PVC 150 -1,271 5.19 P-4 82 8 PVC 150 1,558 9.94 P-5 5 8 PVC 150 750 4.79 P-6 292 6 PVC 150 808 9.17 P-RES1 11 10 PVC 150 287 1.17 P-_RE S2 11 10 PVC 1 150 1,271 5.19 Exhibit F WaterCAD Analysis Summary Junction Analysis - Fire Flow for Commercial Building - 1,500 gpm - FH Junction Elevation (ft) Total Demand (gpm) Pressure (psi) EXISTING FH 1 332 0 45 EXISTING FH 2 329 0 45.9 J-1 337 0 42.3 J-2 338 0 42.4 J-3 338.7 0 40.5 PROPOSED FH 1 338.7 1,500 40.4 PROPOSED FH 2 343.1 58 38.5 Exhibit F WaterCAD Analysis Summary Pipe Analysis - Fire Flow for Commercial Building -1 500 gpm - FH 1 Pipe Number Length (ft) Size (in) Material Hazen- Williams C Flow (gpm) Velocity NO P-1 651 8 PVC 150 287 1.83 P-2 496 10 PVC 150 287 1.17 P-3 144 10 PVC 150 -1,271 5.19 P-4 82 8 PVC 150 1,558 9.94 P-5 5 8 PVC 150 1,500 9.57 P-6 292 6 PVC 150 58 0.66 P-RESl —ES 11 10 PVC 150 287 1.17 P-R2 11 10 PVC 150 1,271 5.19 General Information Location: Wellborn Business Park is located on McCullough Road, east of Wellborn Road. General Note: A 10" water line will connect to the existing 10" water line along McCullough Road. An 8" waterline will connect to the 10" line and extend into the property. Land Use: Commercial/Office Design Criteria/Analysis Primary Water Supply: Existing 10" water line along the McCullough Road. Domestic Demand: Max. Demand Flow: 58.4 gpm See Exhibit C - Fixture Unit Count Fire Flow: 1, 750 gpm — Maximum building is 4000 sf. for type V-B Construction, the required flow is 1,750. A flow test from an existing hydrant was used to compute the residual pressure to use in the WaterCad computer model. Flow Hydrant: Proposed FHI & FH2 Flowrate: 875 gpm each Exhibits: Exhibit A — Water System Layout Exhibit B — Water System Fire Hydrant Flow Test Report Exhibit C — Fixture Count Determination Exhibit D — Pipe and Junction Analysis — Domestic Demand Exhibit E — Pipe and Junction Analysis — Fire Flow Demand Conclusion The proposed 10" & 8" water lines are in accordance with the BCS Water Design Guidelines. This report provides the results of the water system analysis under the fire flow & domestic conditions for the proposed commercial buildings. The pressure and velocity values are computed by the WaterCad software. The lowest residual pressure in the system with the fire flow and domestic demands (1,808 gpm) is 37.5 psi. The lowest residual pressure in the system with only the domestic demand (58 gpm) is 54 psi. Each of these pressures exceeds the 20 psi and 35 psi minimum pressure requirements. The maximum velocity in all pipes is less than 12 fps. The maximum velocity in the system will be 7.39 fps in 10" pipe P-4 with a fire flow of 1,750 gpm. Li THE GARDENS SUBDIVISION EXISTING 10- WATERLINE ih a WELLBORN LANDING SUBDIVISION /EXISTING EXISTING FH 1 EXISTING 10- WATERLINE PROPOSED FH 11 J-3 PROPOSED WATERLINE PROPOSED FH 2 WELLBORN BUSINESS PARK Schultz Engineering, LLC T— WELLBORN BUSINESS PARK"— COLLEGE STATION, TEXAS WATERLINE LA YO UT..w.._ SCALE " ° - ��1L-t4L """m aww n o.a. in xcr ,wa �f-fay rta mts EXHIBIT B SCHULTZ ENGINEERING, LLC FIRM #12327 WATER SYSTEM FIRE HYDRANT FLOW TEST REPORT Date: June 30, 2009 Water System Owner: Wellborn SLID Development Project: Wellborn Landing Subdivision —Wellborn, Texas Flow Test Location: Fire Hydrant on McCullough Road Nozzle size (in.): 2.5 Pitot Reading (psi): 55 Flowrate (gpm): 1,245 Discharge Coeff: (c) = 0.90 Flowrate Formula: Q=29.84cd2p1/2 c = discharge coeff. d = orifice size (in) P = pitot pressure (psi) Pressure Gauge Location: Fire Hydrant at the Intersection of Live Oak and Church Static Pressure (psi): 60 Residual Pressure (psi): 56 Computed Discharge at 20 psi Residual Pressure: QR = 4,330 gpm Discharge Formula: QR = QF X (hr0.54/hf .54) Note: The flow test and report were prepared in accordance with NFPA 291. Report Prepared by: Joseph P. Schultz Others Present: Stephen Cast — Wellborn SLID Exhibit C Fixture Count Determination (Plumbing Code) Fixture Unit Value Fixture Type # of Fixtures Load Factor Fixture Units Water Closet 1 5 5 Lavatory 1 2 2 Service Sink 1 3 3 Total = 10 *Demand = 14.6 GPM *The demand is calculated per building. There will be 4 buildings for a total domestic demand of 58.4 Exhibit D WaterCAD Analysis Summary Junction Analysis - Domestic Flow for Commercial Building Junction Elevation (ft) Total Demand (gpm) Pressure (psi) EXISTING FH 1 332 0 58.8 EXISTING FH 2 329 0 60.1 J-1 337 0 56.7 J-2 338 0 56.2 A 338.7 0 55.9 PROPOSED FH 1 338.7 0 55.9 PROPOSED FH 2 343.1 58 54 Exhibit D WaterCAD Analysis Summary Pipe Analysis - Domestic Flow for Commercial Buildine Pipe Number Length (ft) Size (in) Material Hazen- Williams C Flow (gpm) Velocity (ft/s) P-1 651 8 PVC 150 11 0.07 P-2 496 10 PVC 150 11 0.04 P-3 144 10 PVC 150 -47 0.19 P-4 82 10 PVC 150 58 0.24 P-5 5 10 PVC 150 0 0 P-6 292 8 PVC 150 58 0.37 P-RES1 11 10 PVC 150 -11 0.04 P-RES2 11 10 PVC 150 47 0.19 Exhibit E WaterCAD Analysis Summary Junction Analysis - Fire Flow for Commercial Building - 1,750 gpm Junction Elevation (ft) Total Demand (gpm) Pressure (psi) EXISTING PH 1 332 0 45 EXISTING PH 2 329 0 45.8 J-1 337 0 42.2 J-2 338 0 42.4 J-3 338.7 0 40.9 PROPOSED PH 1 338.7 875 40.9 PROPOSED PH 2 343.1 933 37.5 Exhibit E WaterCAD Analysis Summary Pipe Analysis - Fire Flow for Commercial Buildine -1.750 Rom Pipe Number Length (ft) Size (in) Material Hazen- Williams c Flow (gpm) Velocity (ft/s) P-1 651 8 PVC 150 333 2.12 P-2 496 10 PVC 150 333 1.36 P-3 144 10 PVC 150 -1,475 6.03 P-4 82 10 PVC 150 1,808 7.39 P-5 5 10 PVC 150 875 3.57 P-6 292 8 PVC 150 933 5.96 P-RES1 11 10 PVC 150 -333 1.36 P-RES2 11 10 PVC 150 1,475 6.03 UNRIM, SCHULTZ ENGINEERING, LLC FIRM #12327 WATER SYSTEM FIRE HYDRANT FLOW TEST REPORT 12-17-13 Date: Water System Owner: _Wellborn SUD Development Project: Wellborn Business Park Flow Test Location: Wellborn Business Park FH # 2 Nozzle size (in.): _2.5_ Pitot Reading (psi): 46 1140 Flowrate (gpm): _ Discharge Coeff: (c) = 0.90 Flowrate Formula: Q=29.84cd2p1/2 c = discharge Coeff. d = orifice size (in) P = pitot pressure (psi) Pressure Gauge Location: Wellborn Business Park FH #1 56 Static Pressure (psi): Residual Pressure (psi): 52_ Computed Discharge at 20 psi Residual Pressure: OR = 3734 Discharge Formula: OR = QF X (hr 0.54/hf 0.54) Note: The flow test and report were prepared in accordance with NFPA 291. Report Prepared by: Joe Schultz Deven Doyen Others Present: Clenden Adams — Wellborn SUD Britt Curless