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HomeMy WebLinkAboutCorrespondence E-mail Correspondence From: Wally Urrutia Sent: Monday, December 22, 2014 2:38 PM To: Kevin Ferrer Subject: RE: Shipley Do Nuts @ Caprock Crossing (SP 14-299) Good afternoon, I made comments on it Thursday of last week stating we are okay. I will double check on the system for the comments, but we are ok. Thanks. From: Kevin Ferrer Sent: Monday, December 22, 2014 2:28 PM To: Wally Urrutia Subject: Shipley Do Nuts @ Caprock Crossing (SP 14-299) Hi Wally, I'm currently reviewing Shipley Do-nuts at Caprock Crossing (SP 14-299). I've noticed that you didn't have comments regarding this site plan. I just wanted to confirm that radii (20 feet) for the turn next to dumpster pad is sufficient for you guys to turn since FD won't be needing to turn there. Thanks, Kevin Ferrer, EIT Deven Doyen From: Stephen Cast <wsud.sc@verizon.net> Sent: Monday, February 16, 2015 1:24 PM To: Deven@schultzengineeringllc.com Subject: FW:Wellborn Water Line at Shipley Do Nuts - Caprock Crossing Attachments: image001jpg; 14-360 WELLBORN WATER C6 (1).pdf Deven, Wellborn Special Utility District approves the attached site plan with the 16" water line relocation on the Shipley project. Stephen Cast From: Deven Doyen [mailto:deven@schultzengineeringllc.com] Sent: Monday, February 16, 2015 10:45 AM To: 'Stephen Cast'; 'Jesse Durden CRT' Cc:joeschultz84@verizon.net Subject: Wellborn Water Line at Shipley Do Nuts-Caprock Crossing Stephen, Attached is the revised plan showing the relocated 16" Wellborn SUD water line and the adjustments to the site. If you are good with the revisions please send me an email approving the site plan and associated water relocation, so we can get this processed through the City of College Station. This is the last item to be resolved with them. Thanks, Deven Doyen, P.E. Civil Engineer Schultz Engineering, LLC 2730 Longmire Drive,Suite A College Station, TX 77845 (979)764-3900—Office (979)764-3910—Fax deven@schultzengineeringllc.com 1 Sch- u-1tz Engineering, LLC FIRM #12327 WATER SYSTEM FIRE HYDRANT FLOW TEST REPORT Date: 01/13/15 Water System Owner: Wellborn SUD Development Project: Caprock Crossing Phase 5 Flow Test Location: FH at end of line. Nozzle Size (inch): 2.5 Discharge Coeff (c) = 0.90 Pitot Reading (psi): 64 Flowrate Forula: Q=29.84cd2p1/2 Flowrate (gpm): 1342.8 c = discharge coeff. d = orifice size p = pitot pressure (psi) Pressure Gauge Location: FH in middle parking island Static Pressure (psi): 81 Residual Pressure (psi): 65 Compute Discharge at 20 psi Residential Pressure: QR = 2766 Discharge Formula: QR = QF x (hr0.54/hf0.54) Note: The Flow Test and Report were prepared in accordance with NFPA 291 Report Prepared By: Deven Doyen "'I�.)� ‘ Ricky Flores � of T 9s�1 Others Present: Clenden Adams - Wellborn SUD i*r " *ISI DEVEN L. DOYEN j �. 109835 •4/ �f +�e••�/ S.' • 1I1511ti Proposed TIA Analysis Shipley Do-Nuts at Caprock Crossing Proposed Restaurant W/Drive Thru Tract location: Greens Prairie Road West of Arrington Road Current Land Use—GC Vacant Projected Peak Hour Vehicle Trips per GC Zoning 2.7 Thousand Square Feet x 53.61 Trips per Thousand Square Feet= 145 Vehicle Trips 145 Vehicle Trips< 150 Vehicle Trips TIA not required